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result(s) for
"Tuvesson, Malin"
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Low-Grade Syngas Biomethanation in Continuous Reactors with Respect to Gas–Liquid Mass Transfer and Reactor Start-Up Strategy
by
Lundgren, Anders
,
Arrigoni, Juan
,
Paladino, Gabriela
in
Alternative energy sources
,
Biogas
,
Biomass energy
2023
In order to utilize a wider range of low-grade syngas, the syngas biomethanation was studied in this work with respect to the gas–liquid mass transfer and the reactor start-up strategy. Two reactors, a continuous stirred tank (CSTR) and a bubble column with gas recirculation (BCR-C), were used in the experiment by feeding an artificial syngas of 20% H2, 50% CO, and 30% CO2 into the reactors at 55 °C. The results showed that the CH4 productivity was slightly increased by reducing the gas retention time (GRT), but was significantly improved by increasing the stirring speed in the CSTR and the gas circulation rate in the BCR-C. The best syngas biomethanation performance of the CSTR with a CH4 productivity of 22.20 mmol·Lr−1·day−1 and a yield of 49.01% was achieved at a GRT of 0.833 h and a stirring speed of 300 rpm, while for the BCR-C, the best performance with a CH4 productivity of 61.96 mmol·Lr−1·day−1 and a yield of 87.57% was achieved at a GRT of 0.625 h and a gas circulation rate of 40 L·Lr−1·h−1. The gas–liquid mass transfer capability provided by gas circulation is far superior to mechanical stirring, leading to a much better performance of low-grade syngas biomethanation in the BCR-C. Feeding H2/CO2 during the startup stage of the reactor can effectively stimulate the growth and metabolism of microorganisms, and create a better metabolic environment for subsequent low-grade syngas biomethanation. In addition, during the thermophilic biomethanation of syngas, Methanothermobacter is the dominant genus.
Journal Article
Control of Microthrix parvicella and sludge bulking by ozone in a full-scale WWTP
by
Wijnbladh, Erik
,
Levén, Lotta
,
Tuvesson, Malin
in
Actinobacteria - drug effects
,
Actinobacteria - metabolism
,
Activated sludge
2016
Bulking and rising sludge are common problems in wastewater treatment plants (WWTPs) and are primarily caused by increased growth of filamentous bacteria such as Microthrix parvicella. It has a negative impact on sludge settling properties in activated sludge (AS) process, in addition to being responsible for foam formation. Different methods can be used to control sludge bulking. The aim of this study was to evaluate the dosage of on-site generated ozone in the recycled AS flow in a full-scale WWTP having problems caused by M. parvicella. The evaluation of the experiment was assessed by process data, microscopic analysis and microbial screening on the experimental and control line before, during and after the period of ozone dosage. The ozone treatment resulted in decreased abundance of M. parvicella and improved the settling properties, without impairing the overall process performance. Both chemical oxygen demand (COD)- and N-removal were unaffected and the dominant populations involved in nitrification, as analysed by fluorescent in situ hybridization, remained during the experimental period. When the ozone treatment was terminated, the problems with sludge bulking reappeared, indicating the importance of continuous evaluation of the process.
Journal Article